IOGP Well Control Incident Lesson Sharing #23-8
During a coil tubing clean out run a leak developed at a flange between the quad BOP and stripper assembly. The leak was initially stopped following the appropriate protocol however it continued to occur resulting in the requirement to bullhead the well
to minimize the risk of gas a surface. The coil tubing was successfully recovered from the well and a tensioning system was installed to prevent side loading and future leaks.
The Wells Expert Committee/Well Control Incident Subcommittee believes that this incident description contains sufficient lessons to be shared with the industry. We further encourage the recipients of this lesson sharing to share it further within
their organization.
Following a multi-stage fracture completion, a post-frac clean-out run with coil tubing was performed. Prior to running in the hole all connections had been torqued to the recommended value using hydraulic wrench and pressure tested before the run. When
the coil tubing clean out assembly was at 15,900ft, a fluid leak was observed at a flange between the 4-1/16" stripper and 4-1/16" x 5-1/8" crossover above the quad BOP (Refer to stack up schematic). Operations were stopped and an Emergency Check List (ECL)
protocol performed: the quad BOP was closed, pressure was bled-off and the flange tightened. The leak stopped. Operations resumed and the clean-out run was completed at 16,049 ft.
While initiating pulling out of the hole, a fluid leak was reported from the same flange. Operations were stopped and a further ECL protocol was performed. The leak stopped and pulling out of hole resumed. At 15,844 ft, the flange was again observed to be
leaking and a further ECL protocol was performed, but a limited leak remained.
The situation was assessed and discussed with town, and the decision was made to pull out of hole to surface. A further stop was implemented at 13,000ft as some gas was observed at the leaking flange. The well was circulated to remove the gas. Pulling out
of hole was resumed until the fluid leak was observed to be increasing at 679ft. A ECL protocol was performed and the well bullheaded through the kill line to minimize the risk of gas at surface. Pulling out of hole resumed and the coil tubing was recovered
back to surface.
Figure 1: Schematic of stack up
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