IOGP Well Control Incident Lesson Sharing #23-5
During slot recovery operations on a platform well, a 0.9 bbl gain was observed from the B-annulus while performing a flow-check after cutting the 9-5/8” casing. The flow-check was extended to confirm static well conditions and the gain was interpreted
as fluid u-tubing. Circulation was then initiated, resulting in a gas release at surface and general platform alarm. The well was successfully shut-in on the Annular. Further attempts to circulate the well via choke manifold and MGS were abandoned due to high
gas levels persisting after the MGS. A well test / bleed down package was used to finally kill the well safely.
The Wells Expert Committee/Well Control Incident Subcommittee believes that this incident description contains sufficient lessons to be shared with the industry. We further encourage the recipients of this lesson sharing to share it further within their
organization.
Event occurred during slot recovery of a platform well originally drilled & completed in 1995. Gas released from the B-annulus (13 3/8" x 9 5/8" annulus) following cutting of the 9 5/8" casing string. Initial flow check performed post cut recorded initial
0.9bbls gain and thereafter stable well response (assumed/anticipated in operations as fluid u-tubing between the different fluid hydrostatics present within the well bore). Note: seal assembly removed earlier under closed annular preventer with no indication
of flow from the annulus. The well has a complex history and the platform has had multiple changes of operatorship over the last 20 years.
Original spud date January 1995. Kick taken whilst drilling 12 1/4" interval. Well killed and 9 5/8" run and cemented. No reservoir encountered in 8 1/2" section. Well P&A and sidetracked later in 1995, completed as a production well. Identified as TTRD
candidate and sidetracked through liner in 2004. Well operated until 2008 and shut in. Well suspended via wireline intervention in 2019. Slot recovery commenced in April 2021.
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