During snubbing operations personnel attempted to replace a spool wing valve pressure gauge. Once containment was broken, hydrocarbons flowed from the well for ~ 15 minutes. Please consider the following questions in your review of this incident:
- How does your company verify, record and track barrier status throughout well operations?
- How does your company control work tasks during well operations and what is the minimum threshold for management of change?
- Can you identify areas in your well operations where common field practices have led to the normalization of risks and how can you prevent this in the future?
- Which Human Factors (HFs) were an issue here and how does your company strive to protect itself from these HFs?
- What information should be recorded within a handover? When is it updated? Who updates it? Who issues it? When is it issued and to whom?
IOGP Wells Expert Committee/Well Control Incident Subcommittee believes that this incident description contains sufficient lessons to be shared with the industry. We further encourage the recipients of this mail to share it further within their
organization.
The snubbing unit was rigged up and the pump was lined up and ready to pump 10ppg brine as the working fluid.
Prior to running in hole, as there was no tubing in the well, the supervisor asked two hands to check the pressure in the well, which could be done via a gauge on the tubing spool wing valves.
The crew was experienced and, upon arrival at a location, routinely changed out the pressure gauge for one with a more suitable pressure range for the operation and a preferred type and model. In this incident, changing out the gauge, which required breaking
containment, was not identified as part of the work scope to check the well pressure.
The crew manipulated the valves - one turn open / one turn close with resistance - in an attempt to validate closure and proceeded to remove the gauge. At this point, grease flowed out of the wing, followed by hydrocarbons. Hydrocarbons flowed for ~15 minutes
until the crew started pumping brine. When the brine was pumped, the hydrocarbon flow was displaced by the brine and the flow pressure was reduced.
A junk shot was pumped into the wing approximately 7 hours after the start of the incident, shutting off flow completely. The team then pumped 16ppg OBM to fully kill the well. A packer was set and both side outlet valves were replaced fully securing the
well.
Post incident investigation concluded that the side outlet valves were blocked with debris from prior operations and were prevented from closing fully. It is believed that frac sand formed the blockage.
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