During a coiled tubing nitrogen lifting operation, a 30 foot section of degraded coil was ejected followed by uncontrolled well flow. The well was shut-in after 11 minutes with coiled tubing pipe and blind rams. The investigation showed that the coiled
tubing parted due to excessive corrosion caused by multiple inhibition scenarios which were not identified in the pre-job planning.
The IOGP Well Control Incident Subcommittee believes that this incident description contains sufficient lessons to share with the industry. We further encourage the recipients of this mail to share it further within their organization.
The well was cleaned out using coiled tubing pumping inhibited water and nitrogen.
E-line was run and perforations made.
Coiled tubing was used to stimulate the well using acid. Acid was then bullheaded into the formation and allowed to soak.
Nitrogen lift initiated from below perforations using coiled tubing.
Coil tubing began POOH while continuing to lift with nitrogen.
With the coiled tubing 400' from surface the coiled tubing parted, a 30' section of degraded coil was ejected and uncontrolled nitrogen / well flow ensued until the well was shut-in ~11 minutes later using the coiled tubing pipe and blind rams.
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