During the drilling of top-hole sections on a subsea exploration well, a series of water flows were encountered.
A number of lessons were identified relating to subsurface uncertainties, well planning, and the detection of well flow, whilst operating with a mud recovery system during riserless drilling operations:
1) The importance of understanding and planning for subsurface uncertainties in well operations.
2) Risks associated with the implementation of new technologies in well operations, including the management of risks with crew’s knowledge, skills and ability.
The Wells Expert Committee/Well Control Incident Subcommittee believes that this incident description contains sufficient lessons to be shared with the industry. We further encourage the recipients of this mail to share it further within their
organization.
The top-hole section was drilled to TD with seawater and sweeps prior to displacing to 1.32sg (11ppg) mud. A shallow water flow was encountered during the trip-out but the well was killed using a number of heavy pills up to 1.60sg (13.3ppg). Due to concerns
about the hole conditions the decision was taken to abandon the hole section and re-spud the well.
Drilling the drilling of the new top-hole section a similar mud weight of 1.32sg (11ppg) was used but with a revised plan for a shallower section depth. However, before the revised section depth was reached an unexpected flow was detected. It was necessary
to increase mud weight first to 1.38sg (11.5ppg) and then to 1.47sg (12.2) prior to pulling out of the hole. A decision was then made to change the 28” liner casing depth.
Shortly after drilling out the liner with a 1.43sg (11.9ppg), a mud shallow water flows was encountered. Attempt to kill the well with a 1.51sg (12.6ppg) mud was unsuccessful. Eventually, the flow was controlled with 1.55sg (12.9ppg) mud but with slight
losses occurring.
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