What Went Wrong?:
A rapid increase in flow out was observed. Within 6 seconds, the flow out increased from the drilling rate of 1,600 gpm to in excess of 3,000 gpm. Within the MPD system set-up, the Coriolis meter raw data was evaluated by the system to determine "good" data
versus "bad" data. However when performing this data validation step the Coriolis meter flow out threshold settings considered values less than 0 gpm and greater than 3000 gpm to be "bad" data.
In response to bad Coriolis meter data, the system would use for calculations and display a zero value. Due to this system response, the rig personnel were provided data indications that there was no flow out, when it actually exceeded 3,000 gpm, and the
surface back pressure was observed to be increasing despite a fully opened choke. The initial diagnosis by the crew was a plugged choke.
In addition to providing the rig team with incorrect data, the response of the MPD system to a zero flow out value resulted in the kick detection logic not generating an alarm that a kick had been detected. The flow increased to a value in excess of the
upper range limit, i.e. 3,000 gpm, at which point a zero-flow value was returned, in less time than the kick detection trending period of 20 seconds.
The MPD flow line tied into the rig flow line downstream of the rig’s conventional flow detection system and the mud logging equipment.
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