During operations to recover the tubing, as part of a well abandonment, a sudden release of gas occurred. The well was eventually shut-in and made safe although unfortunately during the incident one of the crew members sustained a painful injury while evacuating from the site.
The investigation highlighted gaps in the implementation of the Management of Change process, in Planning and Procedures and in the Equipment used. It also identified that elements of Human Factors contributed to the incident.
The IOGP Wells Expert Committee/Well Control Incident Subcommittee believes that this incident description contains sufficient lessons to be shared with the industry. We further encourage the recipients of this mail to share it further within their organization.
Immediately after severing the mandrel to release a straddle packer at ~700ft a loud sound was heard, and fluid flow observed. The gas and water release lifted the shooting nipple sitting in the slips in the rotary and one of the split master bushings was ejected from the rotary table, rolled across the rig floor through the V-door and landed on the ground beside the catwalk. The well was eventually shut-in with the blind shear rams via the remote BOP panel.
A service hand fleeing the location, scaled a normally closed gate, fell and fractured his thigh. |