Note: Original alert wording from IOGP Member Company.
While the Bottom Hole Assembly (BHA) was being stripped to the casing shoe, a sudden and total failure of the MPD RCD bearing rubbers occurred thereby causing a rapid loss of the Surface Back Pressure (SBP). This resulted in a loss of the primary well
control barrier (Fluid Hydrostatic Pressure + SBP). After approximately 20 minutes the drilling crew was able to reestablish well control by restoring the Equivalent Circulating Density (ECD) to an overbalance condition. The BHA was then pumped to the shoe
and maintenance activities conducted to replace the RCD bearing and continue with normal operations.
The MPD system was installed with a statically underbalanced MW in hole.
The BHA was being pulled, stripping back to the shoe with surface back pressure against the MPD RCD prior to pumping 2.07sg tripping mud from the shoe to surface. A Surface Back Pressure of ~1000psi was applied.
At 4780m a sudden and total failure of the MPD RCD bearing rubbers occurred resulting in a loss of the SBP and as such a loss of the primary barrier (fluid+SBP) for ~20mins. The well was monitored on the active, while the failure was investigated, before
re-establishing drilling ECD to restore overbalance.
Then the BHA was pumped back to the shoe to change the RCD bearing. No gain volume was recorded but two gas peaks of 8% and 5% were circulated.
|