During Slickline operations on a fixed rig, gas was released above the Slickline BOP. The lower master valve was closed in on the X-mas tree successfully shutting in the flow. The lack of pertinent planning and operations execution, along with
an incorrect well status prior to operations, led to personnel risk exposure at the wellsite.
While rigging up the SAS riser and the Slickline BOP on the X-mas tree on of a well classified as non-eruptive after an eruptivity test, the tubing pressure raised suddenly from 0 to 800 psi. Gas was then released at the 50ft level above the BOP, despite
the swab valve being closed. Slickline operators connected the PCE and closed the lower master valve on the X-mas tree. Operations were then suspended.
|
Disclaimer
Whilst every effort has been made to ensure the accuracy of the information contained in this publication, neither the IOGP nor any of its members past present or future warrants its accuracy or will, regardless of its or their negligence, assume liability for any foreseeable or unforeseeable use made thereof, which liability is hereby excluded. Consequently, such use is at the recipient's own risk on the basis that any use by the recipient constitutes agreement to the terms of this disclaimer. The recipient is obliged to inform any subsequent recipient of such terms.
This document may provide guidance supplemental to the requirements of local legislation. Nothing herein, however, is intended to replace, amend, supersede or otherwise depart from such requirements. In the event of any conflict or contradiction between the provisions of this document and local legislation, applicable laws shall prevail.
|