Drilling 8"1/2 x 9"1/2 hole with 1.30SG mud weight (MW) at 2248m - this mud density is used to drill the top section shales for borehole stability purpose.
Crossed an identified sands layer which was expected to be sub-hydrostatic (0.5SG). Observed a connection gas reading up to 60% + pack off tendency. Increased mud weight by step to 1.35SG but gas reading were still high.
Decided to Shut the well in and observed pressure in the well SIDP 400 psi - SICP 510 psi.
A Gain of +/- 10m3 was estimated later (by postmortem analysis of the previous pipe connection and pump-off logs).
Performed Driller's Method and killed the well by displacing 1.51 SG kill mud. Open hole collapsed during circulation with the consequence of string getting stuck and kick zone isolated.
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