What Went Wrong?:
Total depth of the water injector is 4242m MD/ 2661m TVD at ~ 70 degrees in the target sand with 3 oil bearing sands and reservoir pressure 6.5-7.4 ppg EMW.
Lower completion screens were run, and the well circulated to 8.8 ppg brine (~575 psi OB).
An attempt to set a retrievable bridge plug for the lower isolation near the completion packer was unsuccessful.
The lower retrievable test packer with storm valve was set at 2505m (57 deg) with 287m of tail pipe (1085m above the gravel pack packer). The retrievable test packer was set at this depth to allow running the required amount of tail pipe to achieve 30klbs
weight below (tail pipe) and prevent the retrievable test packer from unseating.
Loss rate prior to setting retrievable test packer was ~8 BPH.
Due to high loss rates of 200 BPH upon unseating the retrievable test packer, it was not recognized that hydrocarbons had migrated into the wellbore below it and were rising up the annulus while circulating out. Hydrocarbon migration had been anticipated,
but it was incorrectly assumed that the losses were effectively sweeping the hydrocarbons in the formation. The high-angle of the hole likely allowed gas to migrate up the high-side of the well during this event.
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