P&A Operation on Gas Injector well
Semisubmersible in 318m water depth.
Course of events:
Annulus filled with 1.32 sg brine and tubing with approximately 1.2 sg. Performed flow check prior to punching tubing - well stable.
Observed increase in trip tank shortly after punching tubing. Some return was expected due to different fluid density.
Closed UAP and LAP after gain of 2 m3. Trip tank volume continued to increase and it was decided to close BSR and cut wireline.
Gas level increased to 82%LEL in rotary table on drill floor. This activated the rig ESD1 (20%) and ESD2 (60%).
Well was monitored with closed BSR and UAP. The pressure stabilized at 8 bar. Gas level in rotary decreased to 1-2% LEL.
After several hours with stable pressures, gas in BOP was circulated out. UAP and BSR were opened without observation of more gas. Performed flow check - well stable.
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