After several attempts and a dedicated leak detection run, the 7” and 5” x 4-1/2” liner were inflow tested successfully to max difference of +10 bar.
Ran completion in heavy brine and displaced well to packer fluid (underbalanced).
Rigged up wireline pressure control equipment to install plug and prong in tubing tailpipe. While RIH with the plug on WL, a sudden pressure increase was observed in the well. Pressure increased to 125 bar on the tubing side.
Attempted to bleed off pressure, but pressure increased to 125 bar immediately.
Continued operation to install plug, pressure up tubing and set production packer.
Performed pump and bleed operation to remove gas from A-annulus. The general gas alarm was triggered during his operation due to losing the liquid seal on the poorboy degasser.
Continued pump and bleed operation until no pressure on tubing and A-annulus side, and the tubing and A-annulus were tested successfully.
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